用Fanuc機器人進行上下料試驗,在抓取有序排列的工件時,用了一段碼垛指令;在放置工件時,又用了一段碼垛指令,最后發(fā)現(xiàn)兩段碼垛指令的寄存器出現(xiàn)了干擾。已采用了不同的代碼編號,程序如下:, Q$ x: T8 z& K* {8 {
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1:L P[1] 100mm/sec CNT50 ' H3 ]% j$ p& Z& v# W! D7 S, k
2: L P[2] 100mm/sec CNT50 - q+ f( U! x1 X- ]6 M; u
3: LBL[1]
/ V3 |- _8 T+ d; e4: L P[3] 50mm/sec FINE
. g) S! u8 A G: b5: PALLETIZING-B_1 //抓取零件的碼垛指令// & J9 o1 R* O7 m3 i" H& l
6: J PAL_1[A_1] 30% FINE . O# Q8 @: n# t3 q- V
7: J PAL_1[BTM] 10% FINE 3 A6 S% f2 \; y
8: DO[4:ON:SUCTION]=ON //氣缸吸氣,抓取工件// " L8 q9 Q" f& h3 H
9: WAIT 1.50(sec)
3 H6 X+ n2 g2 F7 X7 j2 `10: J PAL_1[R_1] 30% FINE
$ X; M5 t4 `# C! U2 B# F1 H9 x3 n11: PALLETIZING-END_1
; N' m4 ~( h5 Z9 ^/ l8 E12: J P[4] 80% FINE
7 [: ?* e# W4 A13: J P[5] 80% FINE # S8 D) `4 Z* ?8 @7 n6 Z# \) E
14: J P[6] 50% FINE 9 h$ w) H/ X o# |9 |
15: PALLETIZING-B_2 //放置零件的碼垛指令// ; W$ P; p, x' p
16: J PAL_2[A_1] 30% FINE : ?% t0 q5 }; _3 ?( ]4 x' F3 `
17: J PAL_2[BTM] 10% FINE
" D4 _( w1 A" M1 v18: DO[4:ON:SUCTION]=OFF //氣缸停止吸氣,放置工件// , |( E/ `1 J8 `" z
19: WAIT 1.50(sec) . ]' o# i* D8 C4 w: W1 p0 v9 A. \
20: J PAL_2[R_1] 30% FINE
( T- u# `- g5 A21: PALLETIZING-END_2
2 ~0 }9 [# I( S [22: J P[7] 100% FINE
4 m' [3 k! t$ C" [# K/ I9 e. K23: JMP LBL[1] 4 ]. X2 l8 |$ a8 x5 `! m+ }1 D
[End]
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