用Fanuc機器人進行上下料試驗,在抓取有序排列的工件時,用了一段碼垛指令;在放置工件時,又用了一段碼垛指令,最后發(fā)現(xiàn)兩段碼垛指令的寄存器出現(xiàn)了干擾。已采用了不同的代碼編號,程序如下:
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1:L P[1] 100mm/sec CNT50
( U# \/ x$ v: I: D3 A6 Y3 ~2: L P[2] 100mm/sec CNT50 . X% T: G; N9 Q# U8 G) R/ [* S t9 K, P
3: LBL[1]
; k$ L8 G( Q* C# f& b9 r6 ?4: L P[3] 50mm/sec FINE
3 n# Y; A3 z( ^8 o$ z, E5: PALLETIZING-B_1 //抓取零件的碼垛指令// $ Z0 q; r. @+ p6 v
6: J PAL_1[A_1] 30% FINE 8 t; P8 I% ~& ?, E
7: J PAL_1[BTM] 10% FINE ; x' l5 ~. z( G; M1 J4 K K$ f
8: DO[4:ON:SUCTION]=ON //氣缸吸氣,抓取工件// ! e% _! y: I( I9 t
9: WAIT 1.50(sec) ; Y: M" [7 L' n% S5 A9 ~
10: J PAL_1[R_1] 30% FINE * {9 w& C( z( Q! ]. l
11: PALLETIZING-END_1
# f0 E( @; m% u& P% P6 a) h$ c12: J P[4] 80% FINE
% O- u- N" Z( ?& E2 e5 X% f13: J P[5] 80% FINE 0 ~8 Z) g9 d- \ k1 Z6 ]4 Z. E
14: J P[6] 50% FINE
$ A8 ]! E. R* @1 |% L5 U* j15: PALLETIZING-B_2 //放置零件的碼垛指令// % R: u- |# [7 |0 P" A
16: J PAL_2[A_1] 30% FINE
8 K9 L/ ^: a+ b* ?17: J PAL_2[BTM] 10% FINE
7 I# O7 f+ m/ |$ Q: T# X18: DO[4:ON:SUCTION]=OFF //氣缸停止吸氣,放置工件//
$ r0 r1 Y8 K$ P19: WAIT 1.50(sec)
! K$ x" Z5 O. x$ A: u- w0 f2 q20: J PAL_2[R_1] 30% FINE
, Z9 l% n: t* s( g _21: PALLETIZING-END_2
$ {& ?+ u& G8 O8 A1 L22: J P[7] 100% FINE
|9 x$ q1 Q% w, P! c23: JMP LBL[1] ' n! {# P. n/ x+ {9 K+ i
[End]
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